节点文献
范厝水电站厂房坝段异常扬压力分析
Analysis of Abnormal Uplift Pressures under the Powerhouse Section in Fancuo Hydropower Station
【摘要】 采用灵敏度现场测试、变化规律定性分析、统计模型定量分析等方法,对范厝水电站大坝厂房坝段坝基防渗帷幕后各测压孔扬压水位异常现象进行了综合分析。分析表明,这些测压孔扬压水位异常,主要是由于进水口部位混凝土内存在与上游水位和测压孔连通的细小裂缝,与上游水位之间不存在明显的关联性,因而不代表厂房坝段坝基防渗帷幕存在缺陷或已被削弱。
【Abstract】 In the powerhouse dam section of Fancuo Hydropower Station,abnormal foundation uplift pressures are observed in pressure holes behind the seepage-proof curtain. Based on the in-situ sensitivity testing,qualitative change analysis,and quantitative statistical analysis,this abnormality problem is analyzed. The results show that small fractures exist in the intake concrete mass and connect the reservoir water and the pressure holes. A weak correlation is found between the reservoir water level and the pressures,which means that the seepage-proof curtain still works well without damages or weakness.
【Key words】 dam; uplift pressure; pressure hole; abnormality; analysis;
- 【文献出处】 水电与新能源 ,Hydropower and New Energy , 编辑部邮箱 ,2016年09期
- 【分类号】TV223
- 【被引频次】3
- 【下载频次】54